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| Jeruk 3 retest successful | |
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Offshore staff A initial drill stem test in Jeruk-3 at 4,939 ¿ 4,978 meters was curtailed after several hours due to a loss of control line pressure. The well was re-tested over the same interval when the control line pressure was restored. The flow test was conducted over a 48-hour period and the well flowed oil at a stabilized rate of approximately 2,750 b/d a GOR of about 320 cf/bthrough a 16/64" choke at a wellhead pressure of 4,500 psi. The flow rate was constrained by surface facility limitations. 6-12-06 Page 1 of 1 |
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